System
|
0600
|
SPB-Alert
|
W
| 服务面板检测到一个错误,需要手动救援SPB 和 SDI。可能的原因有:SDI 的错误的速度编码器
SPB 上缺陷的 E2PROM
SPB 上的电池缺失
按SPB 按钮,REB+DDO 同时,以定位错误源
控制板检测到 SPB 和 SDI 故障. Ssk 可能的原因有: 1.编码器故障 2.SPB 上的 E2 存储器故障 3.电池故障 同时按 SPB 上的 REB+DDO 定位故障原因 Error # 1, encoder A failure (only ...AAA/...AAB) Error # 2, encoder B failure (only ...AAA/...AAB) Error # 4, E2Prom failure Error # 5, battery failure Error # 12, 3 encoder A failure Error # 13, received out of range parameters from TCBC/GECB /RCBII | |
0601
| SPB:TempHTS
| W
| 服务面板过热。
| SPB-Temp
|
0602
| LwssService
| W
| 称重板请求REM。参见称重板故障原因。称重系统请求服务
| |
0603
| Aro Service
| W
| The ARO subsystem (modified SPBC_III) requested “Request For Service” (REM). See ARO
subsystem’s event logging for reason.
| |
0604
| S/WChanged
| I
| 软件变更。SCN 更改
| |
0605
| Update S/W!
| F
| 升级软件!要求更新 GECB 软件
| |
0606
| SpbService
| W
| SPB 请求服务
| |
0607
| /TUM1
| F
| TUM1 missing after run at TOP or active during standstill; (reduced overhead: trig- ger modulcontacts)
| TUM1(1047)
HWY-TYP
|
0608
| /TUM2
| F
| TUM2 missing after run at TOP or active during standstill; (reduced overhead: trig- ger modulcontacts)
| TUM2(1048)
HWY-TYP
|
0609
| /TDM
| F
| TDM missing after run at BOTTOM or active during standstill; (shallow pit: trig- ger modul contacts)
| TDM(1049)
HWY-TYP
|
0610
| /TUPS
| F
| TUPS missing during run; (reduced overhead: trigger modul power supply)
| TUPS(1050)
HWY-TYP
|
0611
| /TDPS
| F
| TDPS missing during run; (shallow pit: trigger modul power supply)
| TDPS(1051)
HWY-TYP
|
0612
| SOS up
| F
| Safety Operated Switch Up triggered
| SOSU(1054)
HWY-TYP
|
0613
| SOS down
| F
| Safety Operated Switch Down triggered
| SOSD(1055)
HWY-TYP
|
0614
| PRBB BatLow
| W
| The battery of the PRBB board is weak: During PowerOff, the battery only pro- vides power for
less than 10 seconds.
| EN-PRBB=1
|
0615
| PCB Certi
| W
| The PCB certification is not performed by using OEK PDA until the specified days expired. In order
that this function is ap- plied, it should be set by OEK PDA. Note: only for Korea application
| |
0616
| C-circuit
| F
| C-circuit does not work correctly
Note: only for MCS310
| C-CHK (704)
|
0617
| RBU-Selftst
| F
| Selftest of Rope Brake has failed (i.e. lasted longer than 5 seconds).
Car is blocked until TCI/ERO is switched.
| RBTC (1029)
RBTE (1028)
|
0618
| RBU-Fault
| F
| Rope Brake has detected overspeed. Car is blocked until TCI/ERO is switched.
| RBTC (1029)
RBTE (1028)
|
0619
| HWY-TYP
| F
| Please refer to blinking message “LOPIT cfg!”
| Low Pit
|
0626
| DeepBattery
| F
| LVA Switch or Evolux: Deep Discharge Protection switched off the OCB to pro- tect the batteries
(voltage was < 40 VDC).
| GECB-LV DRV-TYP
|
0627
| LowBat wait
| F
| LVA Switch or Evolux: Enforced Battery Charging
| GECB_LV DRV-TYP
|
0628
|
NoPowerWait
|
F
|
LVA Switch or Evolux: BatRun-T expired during blackout
| GECB-LV DRV- TYP
BatRun-T
|
0629
| HighBatWait
| F
| LVA Switch: Enforced Battery Discharg- ing
Battery voltage exceeded 70 VAC.
| GECB-LV
|
0630
| OverBat
| F
| LVA Switch: Overvoltage Protection is going to switch off the OCB to protect the batteries
(voltage > 75 VDC).
| GECB-LV
|
0631
| E2P Mapped
| I
| The LCB2/TCBC E2Prom data, provided by an E2TB (E2prom Transfer Board) were mapped to the
GECB layout
| |
event
|
0701
|
SP missing
|
F
| Node Guarding does not detect the SP at the CAN bus. Check CAN_OK LED at SP;
Check CAN wiring between GECB & SP;
| |
0702
|
BCB missing
|
F
| Node Guarding does not detect the 1st BCB at the CAN bus. Check CAN_OK LED at LVPB/BCB_II
Check CAN wiring between GECB & LVPB/BCB_II
| |
0703
|
BcbIoFail
|
F
| The state of inputs was not received eve- ry second or the output command was not acknowledged.
CAN bus overload?
Defect LVPB/BCB_II?
| |
0704
| BcbHwFail
| F
| The BCB published an EEPROM error.
Exchange LVPB/BCB_II
| |
0705
|
BcbSwFail
|
F
| The BCB published a task timing prob- lem.
See subcode ‘x’ for details
Exchange LVPB/BCB_II according to subcode
| |
0706
|
EncoderFail
|
F
| The rescue encoder generates no signals during a normal run. Check rescue encoder wiring;
Replace rescue encoder or GECB_II;
| |
0707
|
OCB fail
|
F
| The OCB auxiliary contacts are wired incorrectly. Check wiring to OCB;
Check OCB;
Check GECB_II inputs;
| |
0708
|
Overspeed
|
W
| The measured rescue encoder speed is 15% faster than the nominal speed. The OS contact or the safeties could be acti- vated. MRO is prevented.
Reset OS contact;
Check Encoder / Speed parameter;
|
SPEED
Encoder
|
0709
|
MRO_BRK Flt
|
F
| A wrong voltage at the brake was detect- ed.
That means that the brake could be unin- tentionally lifted during MRO. Check input MRO_BRK and wiring of the brake
Check LVPB / Replace LVPB
DO NOT PERFORM MRO!!!
|
LVA
|
0710
| No Battery
| F
| The 1st BCB misses the rescue battery.
Check RPS / battery
| |
0711
|
BatTempErr
|
W
| The 1st BCB indicates that the battery cannot be charged, because the tempera- ture is out of range.
Check battery temperature sensor
|
|